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Asset Saves

Explore our asset saves showing how minimal efforts can achieve maximum rewards.

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Oil Analysis
Plastics

Extruder Gearbox

Observation

The lubricant is dirty and showing extreme wear. The number of iron particles is 785 and should be 25 or less. The lubricant is listed as an AGMA 6 which should have a viscosity of 320 but it measures 265 cSt. There is a high PQ index indicating large amounts of ferrous materials being removed. The amount of water has tripled since the last sample. The additive package has changed significantly indicating this is not the same lubricant previously tested.​

Recommendation

CME asked customer to verify the lubricant and recommended a hot oil flush to remove the large amount of wear metals and refill with the correct lubricant. If that is not possible, the lubricant should be changed and a filtration system should be attached and filter with a 7 micron beta 1,000 filter.​

Resolution

The customer changed the correct oil and 336 hours of downtime were prevented.​

$
897,600
Savings
336 Hrs.
Downtime Prevented
Vibration - Continuous
Pulp, Paper & Packaging

Flexo Folder Gluer

Observation

There were high-frequency peaks with harmonics in the upper-frequency range of the motor ODE. There was also high SCR firing frequency peak at 21,560 CPM. This could indicate an issue with the brushes.

Recommendation

The CME suggested blowing brush dust out of the motor, checking brushes and springs for proper wear and tension, and inspecting the armature for any issues.

Resolution

The customer cleaned and lubricated the motor and replaced the brushes, which saved 12 hours of downtime and $38,000.

$
38,000
Savings
12
Downtime Prevented
Vibration - Continuous
Chemicals

Off-Gas Fan

Observation

The vibration data points indicated rotating looseness and the fan ODE side had a high 2x in the axial position. 2x running speed is an indication of an alignment issue.

Recommendation

The CME recommended checking the bearings and alignment at the next available downtime.​

Resolution

The customer changed out both DE and ODE bearings, which avoided a failure and 64 hours of downtime.

$
168,480
Savings
64 Hrs.
Downtime Prevented
Vibration - Continuous
Chemicals

Pump Motor

Observation

There was high frequency haystacking that indicates a possible lack of good lubrication.

Recommendation

The CME recommended greasing both motor bearings.

Resolution

The customer greased the bearings and avoided having to replace the motor.

$
100,000
Savings
4 Hrs.
Downtime Prevented
Vibration - Continuous
Food & Beverage

Compressor

Observation

RMS acceleration readings suddenly spiked on both of the compressor ODE monitoring points. There was an extreme degree of high-frequency harmonics, which could indicate thrust bearing wear.

Recommendation

The CME advised the customer to inspect the compressor for signs of thrust bearing wear and plan for the replacement of the thrust bearings. It was also recommended that If vibration readings continued to climb over the next several days, the compressor would need to be shut down to avoid more extensive damage.

Resolution

The male thrust bearing on the ODE side of the compressor was replaced. Post-replacement, vibration readings returned to the normal range. The customer noted that they saved $150,000 and avoided a shutdown.

$
150,000
Savings
Downtime Prevented
Vibration - Continuous
Mining & Materials

Cone Crusher

Observation

High vibration at crusher speed was detected on the motor, indicating possible sheave misalignment and/or incorrect belt tension.​

Recommendation

The CME recommended inspecting the sheaves for proper alignment and ensuring proper belt tension​.

Resolution

The customer replaced the motor, belts, and sheaves, which saved 24 hours of downtime and $240k.

$
240,000
Savings
24 Hrs.
Downtime Prevented
Vibration - Continuous
Food & Beverage

Agitator

Observation

Condition monitoring engineer observes vibration on agitator ODE, issues maintenance recommendation

Recommendation

Sheaves and belt replaced, but condition monitoring engineer calls out worsening sheave misalignment

Resolution

The sheave pulley bore was found to be too big, and the ODE bearing was hot. Replaced taper lock and bearings. Issue resolved, $150k saved.​

$
150,000
Savings
Downtime Prevented
Vibration - Continuous
Metals & Processing

Main Pot Inductor Blower

Observation

Condition monitoring engineer observes increased amplitude in rotor bar activity with turning speed sidebands, indicating electrical issue​

Recommendation

Condition monitoring engineer issues maintenance recommendations to check all electrical connections and measurements, scan with a thermal gun, and replace the motor if not an external issue.​

Resolution

Motor replaced before failure, customer calls out $250k save​

$
250,000
Savings
Downtime Prevented
Vibration - Continuous
Metals & Processing

Baghouse Main Air Fan

Observation

AI alerts condition monitoring engineer; observes harmonics 1x turning speed and >50 g’s pk-pk at turning speed, indicating excessive looseness.​

Recommendation

Condition monitoring engineer issues maintenance recommendation for to perform lift check on Fan ODE​

Resolution

Excessive wear damage was found (0.025” overall) on the housing and bearing; both replaced, avoiding catastrophic failure ​

$
58,000
Savings
24 Hrs.
Downtime Prevented
Vibration - Continuous
Food & Beverage

Boiler Blower Motor

Observation

AI observes +60°F rapid change on motor ODE​

Recommendation

Condition monitoring engineer issues maintenance recommendation

Resolution

Motor cooling fan sudden failure was detected and repaired​

$
6,600
Savings
Downtime Prevented
Industries Served
11
Daily Wins of All Sizes
$12M+
Issues to Be Detected
100+

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